Research Article

Pullout Test on Fully Grouted Bolt Sheathed by Different Length of Segmented Steel Tubes

Table 3

Pullout results for all samples.

GroupsSamplesLinear reaction (Displ.-load)Peak load (kN)Displ. corresponds to peak load (mm)Oscillation timesFinal fract. formNumbers for segments detachmentFinal displ. (mm)

S1 (15 + 5 + 5 + 5)1
29-106157480Bolt fract.264
310-100156490Bolt fract.258

S2 (15 + 5 + 10)17-103157470Bolt fract.165
2
39-104156483Decoupling2129

S3 (15 + 10 + 5)17-107158490Bolt fract.274
28-102159484Decoupling2161
39-105161480Bolt fract.269

S4 (15 + 15)17-104160470Bolt fract.161
29-107161490Bolt fract.166

S5 (9 + 7 + 7 + 7)19-105131230Decoupling244
214-106142431Decoupling292
313-105140420Clamp detachment249

S6 (10 + 5 + 15)18-103153423Decoupling2114

S7 (10 + 10 + 10)18-102153433Decoupling2106
28-103154423Decoupling2110

S8 (10 + 15 + 5)18-102151352Decoupling1102
29-104151372Decoupling192

Pullout tests on them were failed due to the large section of grouping gap between bolt rod and steel tube, which was caused by improper preparation of specimens.